7.2 Troubleshooting
Alarm
No.
1
Alarm Name
Overspeed
2
Main circuit
overvoltage
3
Main circuit
undervoltage
4
Position
overproof
5
Motor overheat
6
Motor stalling
(Table 7.2)
Operation
Cause
Solution
Status
Power on
Driver or motor failure
Replace the driver.
Check parameters
Check whether internal enable
Being enabled
Short circuit between motor and Check the wire of the motor.
UVW
Encoder Position 0 deviation
Motor encoder zeroing
The parameters of the servo incorrect Restore the parameters
During
the Motor connector short circuited
Check that there is no water in the
operation of the
motor connector.
motor
Command speed of too fast
Reduce the command speed.
Acceleration/deceleration unstable
Adjust the acceleration/deceleration
constant.
Load too great
Reduce the load.
Power on
Power supply voltage too high
Reduce the voltage.
Power supply waveform abnormal
Replace the power supply.
Servo driver failure
Replace the servo driver.
In operation
Circuit board failure
Replace the servo driver.
Braking circuit failure
Check the braking resistor.
Being enabled
Main power supply voltage too low Replace the power supply.
Circuit board failure
Replace the servo driver.
Soft start circuit failure
Replace the servo driver.
In operation
transformer capacity insufficient
Increase the transformer capacity.
Power supply wire loose
Tighten wiring terminals
Circuit board failure
Replace the servo driver.
In operation
Command speed too faster
Reduce the command speed.
Input voltage too low
Check R/S/T power supply.
Parameter PA17 too small.
Increase
the
parameter
appropriately.
Wire loose
Check and tighten the wire.
Power on
Motor damaged
Replace the motor.
Sensor wire broken
Check the wire and replace the
sensor.
In operation
Motor power too small
Replace the current motor by a
high-power motor.
Motor interface short circuited
Take waterproof and dustproof
measures.
Servo parameters incorrect
Match a right motor model.
In operation
transmission partially jammed
Disconnect the mechanical part.
Load too great
Reduce the load
Motor failure
Replace the motor.
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